Update dynamixel_io.py - Fix the connexion issue with usb2ax adaptator. #52
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I experienced connexion issue when using ROS package dynamixel_contollers to manage dynamixel motor with usb2ax adaptator. The modification in file dynamixel_io.py solved this issue.
http://answers.ros.org/question/222378/dynamixel-driver-with-usb2ax-issue/